I removed the control panel from the lathe and gave it a quick dose of looking at. Whilst somewhat untidy, it was nevertheless safe. I made a mental note to rewire the panel; it would be fine for an initial test though. I connected a length of blue 2.5mm square "arctic" flex to the appropriate point and terminated this with a blue plug. This flex is designed for outdoor use and can carry 25A maximum. I replaced the panel and plugged in. Here you can see the panel as found with my addition of the arctic flex.
Sharped eyed readers will notice a component missing. When I plugged in the lathe, the lamp worked and the coolant pump motor ran, but the main motor did not. I checked to make sure that all of the interlock microswitches were in the correct state. Still nothing. Now, despite the main and coolant motors being 240 volts, the microswitches and control relays are all 110 volts. This is common industrial practice. Microswitches are not double insulated and as there is more chance of the operator coming into contact with them they are fed from a 110 volt supply. This has its centre tapping earthed to the machine frame. That way the maximum voltage the operator will see, between the frame and a conductor, is 55 volts.
I discovered that this 110 volt supply was absent. I suspected the supply transformer and sure enough its primary turned out to be open circuit. Hence the gap above - I took the photo after removing the offending item. Here is the original transformer.
And another view.
As can be seen, Harrison had every eventuality covered, despite this machine being a 240 volt variant. They clearly just used one transformer type throughout. The primary has tappings for 380 and 440 volts, voltages normally found in ship systems. I knew that Harrison supplied to HM Forces, and later discovered the M250 was common on Royal Navy vessels. The 12 volt secondary was unused.
I now had to find a replacement transformer of the same rating and form factor. Obviously a direct equivalent wasn't a problem; I didn't need all the tappings for the different mains inputs, nor did I need a 12 volt secondary. The trusty manual showed the original transformer was 50VA rating and manufactured by Romarsh. Enquiries quickly revealed that this was an obsolete product. I suppose if I had wanted to be a purist I could have had one made, but I just wanted to get the machine working.
I found an off the shelf 240 - 110 control transformer manufactured by a great little company called Douglas Electronic Industries LTD, in Lincolnshire. You can find them here:- http://www.douglas-transformers.co.uk/
If you are reading this and you have a 3 phase machine, do not despair. A 415 - 110 volt transformer is also available. The secondary wiring would be as described above, with the primary connected across two of the phases.
I cleaned and rewired the panel using new equipment cable and fitted the new transformer. Here you can see the finished article.
Note the earthed secondary centre tap. The newly spruced up panel was refitted and a successful test of all the machines functions ensued. It was a great moment.